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Tuesday, June 8, 2010

In Gulf, It Was Unclear Who Was in Charge of Rig

【出展リンク】: http://www.nytimes.com/2010/06/06/us/06rig.html?th&emc=th

New York Times

In Gulf, It Was Unclear Who Was in Charge of Rig


Gerald Herber/Associated Press
Even before the oil spill, ultimate authority on the rig was unclear.



NEW ORLEANS — Over six days in May, far from the familiar choreography of Washington hearings, federal investigators grilled workers involved in the Deepwater Horizon disaster in a chilly, sterile conference room at a hotel near the airport here.
The six-member panel of Coast Guard and Minerals Management Serviceofficials pressed for answers about what occurred on the rig on April 20 before it exploded. They wanted to know who was in charge, and heard conflicting answers.
They pushed for more insight into an argument on the rig that day between a manager for BP, the well’s owner, and one for Transocean, the rig’s owner, and asked Curt R. Kuchta, the rig’s captain, how the crew knew who was in charge.
“It’s pretty well understood amongst the crew who’s in charge,” he said.
“How do they know that?” a Coast Guard investigator asked.
“I guess, I don’t know,” Captain Kuchta said. “But it’s pretty well — everyone knows.”
Looking annoyed, Capt. Hung Nguyen of the Coast Guard, one of the chief federal investigators, shook his head. The exchange confirmed an observation he had made earlier in the day at the hearing.
“A lot of activities seem not very tightly coordinated in the way that would make me comfortable,” he said. “Maybe that’s just the way of business out there.”
Investigators have focused on the minute-to-minute decisions and breakdowns to understand what led to the explosion of the Deepwater Horizon, killing 11 people and setting off the largest oil spill in United States history and an environmental disaster. But the lack of coordination was not limited to the day of the explosion.
New government and BP documents, interviews with experts and testimony by witnesses provide the clearest indication to date that a hodgepodge of oversight agencies granted exceptions to rules, allowed risks to accumulate and made a disaster more likely on the rig, particularly with a mix of different companies operating on the Deepwater whose interests were not always in sync.
And in the aftermath, arguments about who is in charge of the cleanup — often a signal that no one is in charge — have led to delays, distractions and disagreements over how to cap the well and defend the coastline. As a result, with oil continuing to gush a mile below the surface in the Gulf of Mexico, the laws of physics are largely in control, creating the daunting challenge of trying to plug a hole at depths where equipment is straining under more than a ton of pressure per square inch.
Tad W. Patzek, chairman of the Petroleum and Geosystems Engineering Department at the University of Texas, Austin, has analyzed reports of what led to the explosion. “It’s a very complex operation in which the human element has not been aligned with the complexity of the system,” he said in an interview last week.
His conclusion could also apply to what occurred long before the disaster.
Exceptions Are the Rule
Deepwater oil production in the gulf, which started in 1979 but expanded much faster in the mid-1990s with new technology and federal incentives, is governed as much by exceptions to rules as by the rules themselves.
Under a process called “alternative compliance,” much of the technology used on deepwater rigs has been approved piecemeal, with regulators cooperating with industry groups to make small adjustments to guidelines that were drawn up decades ago for shallow-water drilling.
Of roughly 3,500 drilling rigs and production platforms in the gulf, fewer than 50 are in waters deeper than 1,000 feet. But the risks and challenges associated with this deeper water are much greater.
“The pace of technology has definitely outrun the regulations,” Lt. Cmdr. Michael Odom of the Coast Guard, who inspects the rigs, said last month at a hearing.
As a result, deepwater rigs operate under an ad hoc system of exceptions. The deeper the water, the further the exceptions stretch, not just from federal guidelines but also often from company policy.
So, for example, when BP officials first set their sights on extracting the oily riches under what is known as Mississippi Canyon Block 252 in the Gulf of Mexico, they asked for and received permission from federal regulators to exempt the drilling project from federal law that requires a rigorous type of environmental review, internal documents and federal records indicate.

Robbie Brown contributed reporting from New Orleans, and Tom Zeller from New York.

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  • Monday, May 31, 2010

    White House Tries to Regroup as Criticism Mounts Over Leak

    【出展リンク】: http://www.nytimes.com/2010/05/31/us/31spill.html?hp

    White House Tries to Regroup as Criticism Mounts Over Leak


    Jae C. Hong/Associated Press
    A worker left the beach as storm clouds approached in Grand Isle, La., on Sunday.



    This article is by Clifford KraussJohn M. Broder and Jackie Calmes.

    Readers' Comments

    HOUSTON — The Obama administration scrambled to respond on Sunday after the failure of the latest effort to kill the gushing oil well in the Gulf of Mexico. But administration officials acknowledged the possibility that tens of thousands of gallons of oil might continue pouring out until August, when two relief wells are scheduled to be completed.
    “We are prepared for the worst,” said Carol M. Browner,President Obama’s climate change and energy policy adviser. “We have been prepared from the beginning.”
    Even as the White House sought to demonstrate that it was taking a more direct hand in trying to solve the problem, senior officials acknowledged that the new technique BPwill use to try to cap the leak — severing the riser pipe and placing a containment dome over the cut riser — could temporarily result in as much as 20 percent more oil flowing into the water during the three days to a week before the new device could be in place.
    “This is obviously a difficult situation,” Ms. Browner said onNBC’s “Meet the Press” on Sunday, “but it’s important for people to understand that from the beginning, the government has been in charge.”
    “We have been directing BP to take important steps,” including the drilling of a second relief well, she added.
    The White House said that Interior Secretary Ken Salazarwould make his eighth trip to the region and that the number of government and contract employees sent to work in areas affected by the spill would be tripled.
    But despite the White House efforts, the criticism also intensified. Colin L. Powell, who served as secretary of state and chairman of the Joint Chiefs of Staff, told ABC’s “This Week” that the administration must move in quickly with “decisive force and demonstrate that it’s doing everything that it can do.”
    Gov. Bobby Jindal of Louisiana, appearing on “Meet the Press,” again criticized the administration’s efforts, saying: “We need our federal government exactly for this kind of crisis. I think there could have been a greater sense of urgency.”
    The administration has left to BP most decisions about how to move forward with efforts to contain the leak. But Ms. Browner made a point of saying that the administration, led by Secretary of Energy Steven Chu, had told BP that the company should stop the top kill. Government officials thought it was too dangerous to keep pumping drilling mud into the well because they worried it was putting too much pressure on it. BP announced Saturday evening that it was ending that effort.
    BP engineers are now working on several containment plans, with the first being implemented over the next few days.
    “According to BP, the riser cutting will likely start Monday or Tuesday,” the White House press secretary, Robert Gibbs, said in a statement on Sunday.
    Using submarine robots, technicians intend to sever the riser pipe on top of the blowout preventer, the five-story-high stack of pipes above the well that failed to shut off the leak when the Deepwater Horizon rig exploded on April 20, killing 11 workers. A funnel-like containment device will be fitted above the cut riser to draw the escaping oil through tubing attached to a drilling ship.
    But BP officials acknowledged that there was no certainty that this attempt would work. Robert Dudley, BP’s managing director, appearing on “This Week,” also said that if it did work, some oil would still seep out until relief wells provided “an end point” in August.
    The failure of the most recent effort — known as a top kill, which BP officials expressed great optimism about before trying it — has underlined the gaps in knowledge and science about the spill and its potential remedies. Ever since the explosion and the resulting leak, estimates of how much oil is escaping have differed by thousands of barrels a day. Both government and BP officials said on Sunday that they had no accurate idea of how much oil was spilling into the gulf.
    “We honestly do not know,” Mr. Dudley said on “Meet the Press.” “We’ve always found this a difficult oil to measure because of the huge amounts of gas in the oil.”
    “The one thing about this method that we’re about to go into — it will and should measure the majority of the flow,” he said.
    Mr. Dudley said that the original estimates by the government and BP officials of 5,000 barrels a day were based on satellite pictures and that the current estimate of 12,000 to 19,000 barrels was “issued without an actual flow measurement.” If the leak is not contained or slowed and continues at the higher estimated flow rate of 19,000 barrels a day until Aug. 20 — four months after the accident — it could amount to close to 2.3 million barrels spilled into the gulf.
    After more than a month of diagnostic tests and the pumping of tens of thousands of barrels of drilling fluids — and everything from golf balls to shards of rubber — into the broken blowout preventer, engineers are still debating about what they think may be the inner contours of the five-story stack of pipes and how to best contain its leaking gashes.
    In the end, all the mysteries of what went wrong and caused one of the greatest environmental calamities of history may not be known until the well is finally killed and the ill-fated blowout preventer is brought up from the bottom of the sea.
    The final plugging of the well will have to wait until August, when the two relief wells are scheduled be completed. Those wells are being drilled diagonally to intersect with the runaway well and inject it with heavy liquids and cement. Work could be slowed by storms in what is expected to be an active summer hurricane season.
    Officials from BP and the administration announced on Saturday that the top kill was a failure and had been abandoned, and that engineers were once again trying to solve the problem with a containment cap. A similar operation was tried nearly four weeks ago, but it failed because a slush of icy water and gas, known as hydrates, filled the large containment device, blocking the escaping oil from entering it. This time, engineers will pump hot sea water around the new, smaller device to keep hydrates from forming, and there will be far less space between the cap and the well for any hydrates that do form to flow in.
    BP officials expressed optimism on Sunday about the new operation, though one technician working on the project warned that there were concerns that hydrates could again stymie the containment effort. The technician and outside experts also warned that by cutting the riser, the engineers may increase the flow of escaping oil.
    Donald Van Nieuwenhuise, director of petroleum geoscience programs at the University of Houston, said that he thought BP’s next plan had a good chance of succeeding, but that there was also a risk of increasing the flow of escaping oil by 10 percent.
    “Then it just makes the situation worse for longer,” he said, unless the containment cap succeeds in collecting a substantial amount of oil.

    Clifford Krauss reported from Houston, John M. Broder from Washington and Jackie Calmes from Chicago.

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